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Published January 8, 2008 The authors share their experience in debottlenecking a methanol plant at GNFC Ltd. The project involved the commissioning of a state of the art Isothermal reactor from Linde. GNFC is located at Bharuch,
Gujarat India and is engaged in manufacturing
of fertilizers. The key products are urea, ANP, CAN, formic acid, methanol, acetic acid, Brief History - Enhancing
the Methanol-I Plant Capacity Originally, this plant was
designed to operate on feed gas from an ammonia plant consisting of a gas mixture of 75%
hydrogen, 22% carbon dioxide, 1% carbon monoxide and some inerts. The reaction of the methanol in gas rich in CO2
is milder as it produces water along with methanol. The
crude methanol concentration is also lower. Water further retards the rate of reaction.
The two reactions involved here are: H2 + CO2 ---->
CH3OH + H2O
+ 9.8 kcal/kgmol
H2 + CO ----> CH3OH
+
21.6 kcal/kgmol
Normally, a gas mixture of H2
+ CO + CO2 is used in a proportion measured in terms of a R value
(H2-CO2)/(CO+CO2) equal to 2.0 to get an optimum methanol
conversion per pass. Changes to the process
included: 1. A methanol chiller was
introduced in the gas cooling circuit at the reactor outlet to reduce the methanol
concentration and temperature in the recycle gas which helped to increase the methanol
production from 4~5 MTD up to 75 MTD level. 2. Setting up a synthesis gas
generation unit (SGGU) to supply CO rich gas from natural gas reformer in February 1998. This gas composition is better for methanol
production compared to the rectisol wash gas which is rich in CO2. The
synthesis gas and distillation loops were debottlenecked by replacing of some control
valves, installation of exchangers, and other modifications. The capacity was boosted to 100 to 120 MTD. 3. Replacement of the refining
column trays with high capacity Superfrac trays from Kostch Glistch India Ltd in
October 2002. This, along with other
peripheral modifications, were made to increase distillation capacity to 145 MTD. 4. Replacement of the quench
adiabatic methanol convertor to Lindes Isothermal Reactor and debottlenecking of the
distillation loops for higher capacity. The
capacity of the plant was increased to 160 MTD in September 2003. Major advantages of Isothermal
Reactor include: Lower pressure drop in reactor Figure 1 below shows the
temperature profile in the isothermal reactor.
Compared to the expected 160
MTD production capacity, the unit has achieved a stable production level of 185~190 MTD. A flow diagram of the new loop
is shown in Figure 2 below. In this article,
well focus on this latest dimension added to the plant, highlighting the
re-commissioning experiences.
Plant
Re-commissioning with the Isothermal Reactor Following the replacement of the quench reactor with the Isothermal reactor from Linde, the plant was ready for start up. The following details the activities associated with start up after the changes were made. Basic
and Detail Engineering - Design Fundamentals The original plant was designed
by Linde with process licensing from ICI. Linde performed the basic engineering for the
loop modification and the detailed engineering for the new Isothermal reactor. Based on the data for the new design conditions, a
debottlenecking study on the distillation section was carried out in-house by our
Technical Services department. Major
pre-fabrication work and in-plant erection of the loops which were to be replaced was
completed before the final shutdown of the plant. A
shutdown schedule of 11 days was planned. Outline
of the Pre commissioning activities The piping loops were
identified and broken down into various process loops per the P & IDs. The plant was
broadly classified into three independent sections: synthesis loop, makeup gas loop, and
distillation loop. This helped prioritize
tasks such that the synthesis and related loops were made ready first. The loops, which were erected before shutdown, were
prepared for commissioning by flushing / blowing. Based on the service, the plans for
flushing / blowing were prepared and discussed with the mechanical and instrument groups
to streamline the activities. All instruments in the circuit were removed from the lines. The following procedures were
used: For gas lines: Gasket
blowing with plant air was carried out starting from 1.0 barg up to 3.5 barg repeatedly,
until there was no rust / dust in the line. This was followed by nitrogen passivation /
drying. For liquid lines: Air blowing followed by water
flushing was carried out. This was followed by nitrogen passivation / drying. For steam lines: Gradual
warming of the header before insulation was applied for grease removal and rust flushing
through the trap bypass. Then steam blowing
at full capacity was carried out for half an hour by diverting the open end at a safe
location. The header was allowed to cool. This cycle was repeated again till clear
condensate was discharged in the trap bypass. For Running Machines:
There was a pair of process pumps in each service. One pump online and one spare. With the higher capacity, some pumps were replaced
for higher capacity. The main crude feed pumps and refining column reflux pumps were
replaced. With spare pumps, the plant
operation was not interrupted during the pump changes. Each replacement took 12 days and
included the modification of the base, pipeline, motor, and other ancillary pieces. Likewise, four control valves
were replaced via proper coordination between the operations and project teams. The prefabricated loops were also washed or blown
and then dried with nitrogen. These were kept inert and sealed at their ends until they
were to hooked up during the shutdown. This
also helped reduce the pre-commissioning time for the plant. The start-up boiler feed water circulation pump was
commissioned and stabilized prior to shutdown as soon as the errection of the reactor
steam drum system was completed. Both Methanol-I and SGGU
operate independently. It was not necessary
to shutdown SGGU for the commissioning of Isothermal reactor in the Methanol-I synthesis
loop. The natural gas compressors in the SGGU
plant get cooling water from the Methanol-I plant header. Since
cooling tower was to be taken offline, temporary arrangements to supply an alternate water
source was planned to keep the natural gas compressors in the SGGU running. This was implemented prior to shutdown, avoiding a
stoppage of the SGGU plant.
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